Test mount on my rusty spare suspension leg. Fits like it should:Will see how it will perform overall. First painting, then master cyl. replacement to 20v one, and after that I hope I will have real racing brakes ;).
Test mount on my rusty spare suspension leg. Fits like it should:

Time will show, what will be the result.
You can clearly see, that those 4x4 mounts are solid rubber. Russian made things sometimes last very very well, no matter how crude they are made :). The problem is, that the thread is using M10x1.25 pitch (normal mounts use conventional M10, which is 1.5). Also mount heigh, if I want to put it in the old "cup", is almost twice shorter than needed. Will need to think some strong and elegant solution (it will turn to be weak and horrible to make - as usual :D).
After some home brew machining - it is not looking so good:
Will try to improve construction a bit. But it will be later.
But who will make caliper carriers. Now I'm trying to master CAD software, just to draw something for guys, who work with metal...
Cut top of it, to see what is inside. Quite complicated internals:
Dismantled middle part:
Nice pot to fill it with something (nylon? polyurethane?). Will think about it:
Burned remaining rubber with propane torch, however no pictures. It is interesting what would happen if to fill this area with polyester epoxy and glass fiber. Will it crack? We will see ;).

Photos - (C) by Duskin
Everything was fixed and tightened properly. Did a few small jobs (leaks, cable fixings), not worth to mentioning. One which really improved something was adding flexi to the exaust pipe. Measurements:
And flexi welded in place:
Now I'm not loosing exaust (and burning handbrake cables) in the middle of track :). Ok some sound and effects are lost, but at least everything stays in place

Pushed the wires on to the shelf, and vuala - it fits nicelly. No more spaghetti mess at the passenger's legs:
Started to feel and think like zombie. Working for 8-10 hours per day for two weeks - started to bring the results, almost finished car, loads of cuts and bruises on the arms, legs, head... The PAIN in every muscle. Started to use weak analgetics to help the progress...
After a while it started to leak coolant from everywhere - I forgot to tighten few clamps. Starting to get very tired, thus making stupid mistakes. Not good.
Also eliminated dead end for activated charcoal valve (was leaking boost and doing nothing):
Replaced oil pressure sender (one contact VDO to some noname two contact). Reason for this is employing oil pressure check unit fom KV engine. It is using two pressure sensors to operate properly. So I put two contact sender (gauge and warning), and found plug in the block where I managed to put old pressure switch from KV.
Put the radiator in, connected everything on the driver's side:
Bolted driveshafts (took a while , because my measurements were wrong, driveshaft flanges from typ44 are bigger, and I forgot, that I had typ44 flanges on my spare gearbox, which was used as reference - they were given to my friend some years ago). And if you notice, turbocharger went from the floor into engine bay ;)
Also wrote more blog entries with past dates. Had no time to do this before, because my schedule for these two weeks was - eat, sleep, work in the garage, or search for the parts. Enjoy...
New:
There's visible difference of leaf spring height. So decided to use all the stuff (release shaft, bearing, etc. from apropriate type).
Closer look:
So now its time to pull engine out (to change gearbox, flywheel, clutch). Like always, I will do it by dropping engine and gearbox to basement. To achieve this - you need to dismount everything, and leave bare engine. So it started like this:
And in the evening all the hoses, and fluids were out:
It is obvious, that I have sprayed paint somewhere, but not on tubes. Especially in the places where shadows like to be:
Old coupe turbo quattro modification log